Pat Hickey
f1624621b3
ArduCopter Logging: DISABLED means DISABLED again; CONFIG_LOGGING added
...
CONFIG_LOGGING selects LOGGING_SIMPLE and LOGGING_VERBOSE. Verbose
logging is the default, implemented in Log.pde. Simple logging is
optional, but the default for the 1280 build, implemented in
Log_simple.pde
2011-12-19 21:04:51 -08:00
Randy Mackay
310f072d50
Arducopter - added "//#define APM2_BETA_HARDWARE" to AP_Config.h for developer's who received early version of the board with the old barometer
2011-12-19 22:57:00 +09:00
Jani Hirvinen
106801a59c
config settings for jD motors
2011-12-19 09:29:05 +07:00
Jason Short
b53a6bd4b4
Hexa stability patch bug fix by borna.segulin
2011-12-18 16:38:07 -08:00
Jason Short
239eb53983
change Alpha name
2011-12-18 16:38:07 -08:00
Andrew Tridgell
ad9c0533d8
ACM: run mavlink loop while erasing logs
2011-12-18 10:19:41 +11:00
Jason Short
8970948804
Sync logging
2011-12-16 22:02:41 -08:00
Jason Short
47e4c875e1
Cleanup
...
removed Iterm experiment - no noticeable effect in actual flight
2011-12-16 20:47:23 -08:00
Andrew Tridgell
f6f808357c
removed AperiodicProcess code
...
this code was never being used, and was more complex than it was
worth.
2011-12-17 07:29:09 +11:00
Jason Short
2fc25d963d
renamed super simple, added framework for auto calc of throttle cruise
2011-12-15 20:51:41 -08:00
Jason Short
3019c35364
turned off iterm for traverse
2011-12-15 20:51:41 -08:00
Jason Short
f11f2c6d97
added some more throttle imax range
...
renamed Super Simple
2011-12-15 20:51:41 -08:00
Jason Short
72605f846c
renamed super simple
2011-12-15 20:51:41 -08:00
Jason Short
88b3708dcf
added altitude to circle mission
2011-12-15 20:51:40 -08:00
Jason Short
0ba8a9f30b
Allows user to specify just an altitude for Circle Mode
2011-12-15 20:51:40 -08:00
Jason Short
4e280bb0dc
More power to descend
2011-12-15 20:51:40 -08:00
Jason Short
3446744ae9
Addition of nav mode that tries to maintain level
2011-12-14 22:08:42 -08:00
Jason Short
4d90058c90
dupe of landing logic for scripting
2011-12-14 22:08:41 -08:00
Jason Short
f48e394511
made the last step of landing stop navigating so we can drop straight down.
2011-12-14 22:08:41 -08:00
Jason Short
1251e8105d
Added failsafe check
2011-12-14 22:08:41 -08:00
Jason Short
c6657f4a93
updated Loiter control to provide an alternative to GPS rate control for users with circling issues. Works in SIM, needs flight testing
2011-12-14 22:08:41 -08:00
Jason Short
d2fd6c5ee5
added loiter control to reset nav
2011-12-14 22:08:41 -08:00
Jason Short
8691b10ee9
added failsafe check,
...
enable loiter repositioning
2011-12-14 22:08:41 -08:00
Doug Weibel
5d197ae337
Change logging to default on for 2560
2011-12-13 20:53:44 -07:00
Doug Weibel
8b78c4a4c5
Changes to logging file system to avoid problems with 0 and 1 page logs
2011-12-13 20:09:07 -07:00
Michael Oborne
e20d3a3676
add method of detecting if motors are armed
2011-12-14 06:18:29 +08:00
Randy Mackay
7f64080877
Arducopter - Attitude.pde - fixed small bug in pitch stabilise
2011-12-13 22:10:51 +09:00
Andrew Tridgell
483bef35e5
IMU: update ACM and APM for flash_leds change in IMU init
2011-12-13 18:19:41 +11:00
Andrew Tridgell
888d6226b2
fixed two more CONFIG_HARDWARE #ifdef bugs
2011-12-13 17:05:48 +11:00
Jason Short
edc3a731d4
Adjustments for High Wind enviroments
2011-12-12 17:47:45 -08:00
Jason Short
ba8fc57bd8
Stability patch2 - Jose style.
2011-12-12 17:47:45 -08:00
Jason Short
c9b317fc27
Gain updates
2011-12-12 17:47:45 -08:00
Jason Short
f3e408e7e0
Added a simplified Log that is just GPS for my 1280 board
2011-12-12 17:47:45 -08:00
Jason Short
e4559bbf5c
Added param option for Simple mode reset
2011-12-12 17:47:45 -08:00
Jason Short
d83ad1acd4
Upped the max pitch to deal with wind - based on T3 testing
2011-12-12 10:10:33 -08:00
Jason Short
6bc90d6289
Just upped the nav_imax value
2011-12-12 10:10:33 -08:00
Andrew Tridgell
a22893124d
fixed LOGGING_ENABLED default on ArduCopter
2011-12-12 23:40:43 +11:00
Andrew Tridgell
5760239670
quad: fixed the comments on the + motors
2011-12-12 21:01:58 +11:00
Andrew Tridgell
d076fb54b5
fixed barometer detection on APM2
2011-12-12 15:45:36 +11:00
Andrew Tridgell
f5e439554d
fixed == that should be =
2011-12-12 15:19:50 +11:00
Andrew Tridgell
358dc91d41
fixed hil ArduCopter build
2011-12-12 15:14:55 +11:00
Andrew Tridgell
07dba4eff7
desktop: fixed Wire.begin() build problem
2011-12-12 15:14:55 +11:00
Andrew Tridgell
1b1c629167
added sitl build target
2011-12-12 15:14:55 +11:00
Andrew Tridgell
011110e1dd
airspeed: use floating point values and better averaging in zero_airspeed()
...
this makes the calibration of airspeed a bit more accurate, and
prevents truncation of airspeed values
2011-12-12 15:14:55 +11:00
Pat Hickey
a48c65b5b5
ArduCopter: update AP_Baro constructors & initializers
2011-12-11 15:21:10 -08:00
Pat Hickey
f3ad7f3af8
Wire and SPI Init: move to sketch system.pde from libraries
...
* Wire.begin removed from AP_Baro_BMP085::init()
* SPI.begin removed from AP_Baro_MS5611::init()
* SPI.begin removed from AP_InertialSensor_MPU6000::hardware_init()
* Both Wire.begin and SPI.begin added very early in init_ardupilot in
ArduCopter/system.pde and ArduPlane/system.pde
2011-12-11 15:21:10 -08:00
Pat Hickey
6dbd6b4181
ArduCopter: Get barometer data in terms of AP_Baro interface
...
* Major change: Log.pde Log_Write_Control_Tuning has changed significantly
* MS5611 has no concept of RawPres and _offset_press
* Log the get_pressure() instead. (If we don't trust the barometer, what's the point?)
2011-12-11 15:21:10 -08:00
Pat Hickey
39fe9075d9
ArduCopter Init: different call to barometer.init based on CONFIG_BARO
...
* BMP085 has two arguments, second varying on apm1/apm2
* ms5611 has no arguments
2011-12-11 15:21:10 -08:00
Pat Hickey
b055aa6f81
ArduCopter: instantiate correct AP_Baro object based on CONFIG_BARO
2011-12-11 15:21:09 -08:00
Pat Hickey
d7f77aec93
ArduCopter & ArduPlane: Added support for apm2beta build via APM2_BETA_HARDWARE define
...
* This enables the BMA085 driver for compatibility with beta boards.
* The CLI_SLIDER_ENABLED=DISABLED line does not need to be in the makefile.
config.h takes care of this default.
2011-12-11 15:21:09 -08:00
Pat Hickey
62844d8ddc
ArduCopter: added config.h and defines.h to support CONFIG_BARO
2011-12-11 15:21:09 -08:00
Pat Hickey
de6507a47d
ArduCopter: Rename APM_BMP085 classes to AP_Baro_BMP085 classes.
2011-12-11 15:21:09 -08:00
Pat Hickey
8d878a2cae
ArduCopter CLI: Add imu.init before imu.init_accel for "level"
...
* Depending on when you entered the CLI, the imu might not be
initialized yet, and init_accel would hang.
2011-12-11 15:19:46 -08:00
Pat Hickey
2e200834e1
ArduCopter: Revert "Switched to Gyro only startup"
...
This reverts commit f932f0a9f6a29e9c3193622109298c657ed5a908.
I fixed this bug in 734185599cd9d6a487c675460c09895172e012b0.
It is no longer valid to call IMU::init_gyro() before IMU::init().
2011-12-11 14:50:02 -08:00
Jason Short
5d0e3664ad
Hack to prevent fly aways
...
Cleanup to remove SIMPLE mode switch note
2011-12-11 12:01:06 -08:00
Jason Short
e8e126a636
removed CLI switch by default, decreased Nav I
2011-12-11 09:53:44 -08:00
Jason Short
c1aa015ef1
added debug prints, broke out Angle val to debug
2011-12-11 09:53:44 -08:00
Jason Short
a685e5b575
fix for navigation scaleLongUp
2011-12-11 09:53:44 -08:00
Randy Mackay
fe336fb749
ArduCopter - small fixes to fix HIL compile errors
2011-12-11 23:25:03 +09:00
Randy Mackay
67855b207d
Arducopter, RangeFinder - added SONAR_TYPE parameter and properly support the XL (default), LV and long distance XL (aka XLL) sonar types
2011-12-11 16:40:59 +09:00
Jason Short
f89fed02c3
made it so nav is called in Simple mode
2011-12-10 23:31:37 -08:00
Jason Short
4659a9ffce
Adjust Simple mode on the fly.
2011-12-10 23:29:29 -08:00
Jason Short
af0ae6a10f
Set Nav_WP as home
2011-12-10 23:26:10 -08:00
Jason Short
1f3abcf048
eased up on the i term blocker
2011-12-10 23:25:52 -08:00
Jason Short
069bcbf5e6
Made landing slower
2011-12-10 19:33:19 -08:00
Jason Short
873daae095
Allows you to clear the stored mission when in Auto
2011-12-10 19:32:46 -08:00
Jason Short
29554b7d73
Will add a landing command to last WP if we are on the ground.
2011-12-10 19:29:42 -08:00
Jason Short
648ab5f4ae
Switched to Gyro only startup
2011-12-10 15:13:20 -08:00
Jason Short
f3ff7aa0a8
rework of inflight trim.
2011-12-10 15:05:53 -08:00
Jason Short
5e12924907
Removed Instant PWM from disarmed output
2011-12-10 10:33:25 -08:00
Jason Short
0289e35347
Ground course saved as long for SIM compat
2011-12-10 10:19:20 -08:00
Jason Short
84b72b627b
Added SIMPLE mode reset outside of bounding box of 10M, will do more testing before enabling.
2011-12-10 10:19:20 -08:00
Jason Short
7cecca74bc
Made Baro_alt int32_t
...
Added home to copter bearing, home to copter distance
Added Land mode
2011-12-10 10:19:20 -08:00
Jason Short
69f1841d8e
Debugging some motor issues
2011-12-10 10:19:20 -08:00
Jason Short
76d60a2111
Added Home Bearing
2011-12-10 10:19:20 -08:00
Jason Short
d9347290a4
Added notes to Imu.ax, ay, az
2011-12-10 10:19:20 -08:00
Jason Short
2b8280e533
Added enumeration for Land
2011-12-10 10:19:20 -08:00
Jason Short
307723960d
Increased slightly the Auto_trim time
2011-12-10 10:19:20 -08:00
Jason Short
3ff7b047d5
Added Bearing to home, distance to home calcs
2011-12-10 10:19:20 -08:00
Jason Short
49806d93d9
Added Land FLight mode definition
2011-12-10 10:19:20 -08:00
Randy Mackay
0b24914066
OptFlow - turning on optical by default
2011-12-10 23:22:40 +09:00
Randy Mackay
fa0723f115
ArduCopter - removed limitation on Maxbotix sonar type requiring ADC so it can work with APM2.
...
modified default analog pin in test sketch to be AN4 which is consistent with APM2 default
2011-12-10 18:33:30 +09:00
Pat Hickey
cc38189f71
ArduCopter config: Correct LOGGING_ENABLED defaults to force disable for 1280
...
Per email, this is what Jason meant to do in aeb92870, but previous code
forced logging enable for all non-1280 users.
2011-12-09 15:06:10 -08:00
Randy Mackay
4dc2956ca9
Navigatino - small bug fix in loiter controller in which the y_iterm was coming from the Lon controller instead of the lat controller. Found by Sylvain. http://www.diydrones.com/forum/topic/listForContributor?user=18fsncw0k1x6i
2011-12-09 22:13:37 +09:00
Randy Mackay
42421a09e2
TradHeli - Attitude.pde - made yaw contol use jason's stability patch
...
Quad - fixed small bug in pitch control (was using roll's stabilise controller)
2011-12-08 22:23:50 +09:00
Randy Mackay
68e6be5eeb
TradHeli - fixed roll/pitch so it's not scaled when throttle is scaled
2011-12-08 21:30:47 +09:00
Doug Weibel
502a98dda1
Add hook to dump log filesystem index for debugging
2011-12-07 08:13:30 -07:00
Jason Short
6dfdd754ea
Stability patch updates,
...
Cleanup
2011-12-06 21:03:56 -08:00
Jason Short
05409b8c1c
made RateP range a little more sensible
...
removed unused var
2011-12-06 21:03:07 -08:00
Jason Short
a632c49b44
Alt_hold_patch, removed Z dampening from Manual override. Fixed integrator conversion to throttle_cruise
2011-12-04 21:32:33 -08:00
Jason Short
e8a14c8d93
simple patch to improve alt hold based on stability patch
2011-12-04 21:32:33 -08:00
Jason Short
9bc6fce3b8
Function call defs commented with // so the preprocessor doesn't get confused
2011-12-03 17:55:44 -08:00
Jason Short
0d8071a401
Added new gain and clamp value for DCM
2011-12-03 17:55:11 -08:00
Jason Short
54c8e1033c
Fixing reversed Simple mode switch
2011-12-03 17:54:57 -08:00
Jason Short
aad45c692f
Stability patch from 55
2011-12-03 17:54:38 -08:00
Jason Short
778393c4a7
Enabled the compass test
2011-12-03 15:39:02 -08:00
Jason Short
5ed300db7e
disabled Flash logs in 1280 by default
...
Added stability patch I values and limits
2011-12-03 15:38:46 -08:00
Jason Short
c99da66506
Formatting, swicth Omega to raw IMU rates
2011-12-03 15:29:33 -08:00
Jason Short
401c985572
Added Deg to rad, rad to deg * 100 to save a float calc
2011-12-03 15:29:33 -08:00
Jason Short
d7cc241f85
formatting
2011-12-03 15:29:33 -08:00
Michael Oborne
4c61462dfd
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2011-12-04 06:32:27 +08:00
Michael Oborne
edf3195384
add 1hz mavlink loop.
2011-12-04 06:32:08 +08:00
Andrew Tridgell
39a36fe946
fixed the "reboot on GPS lock" bug
...
the problem was that with APM2 we may not have a 2nd GCS instance. The
"gps alt: xxx" message was being unconditionally sent to both GCS
instances, which caused a crash
2011-12-04 09:06:58 +11:00
Andrew Tridgell
aaac6212ab
MAVLink: use the configured system ID for ArduCopter
2011-12-03 07:54:36 +11:00
Jason Short
9931cacec7
Enabled Ch7 simple mode switching
2011-11-28 22:41:12 -08:00
Jason Short
69dd8264e6
adding flag for finished mission
2011-11-28 22:28:51 -08:00
Jason Short
b92b4e9092
cleanup
2011-11-28 21:40:22 -08:00
Jason Short
eb6d34e1fc
Fix error with calc_nav_pitch_roll
2011-11-28 21:27:29 -08:00
Doug Weibel
88ab4f7d70
Fix for intermittent bug of log #1 starting on page 2 and confusing file system
2011-11-28 19:43:10 -07:00
Doug Weibel
b03de3095e
Add DataFlash.Init before doing a forced log erase on eeprom reset.
...
Add progress indication during log erase
2011-11-28 19:42:27 -07:00
Jason Short
b4a0d8a275
Fixed navigation bug
2011-11-28 14:22:05 -08:00
Jason Short
ce5ad442fc
Git Test
2011-11-28 10:54:20 -08:00
Jason Short
62ed256fca
made the crosstrack use the previous WP instead of the current loc to get a better line in AP.
2011-11-28 10:33:06 -08:00
Jason Short
82adf1df6b
removed need to send increment flag to update commands
...
constrained climb_rate value
2011-11-28 10:33:06 -08:00
Jason Short
504b4b52d6
slight refactoring to avoid the increment issue when changing commands
2011-11-28 10:33:06 -08:00
Jason Short
4a6feb3acb
better comments out of some old unused functions to avoid compiler errors
2011-11-28 10:33:06 -08:00
Jason Short
909e5796eb
Logging input to find this freeze bug
2011-11-28 10:33:06 -08:00
Jason Short
df57380adc
Erasing Logs causing major havoc. Users getting infinite loop.
2011-11-28 10:33:05 -08:00
Jason Short
cc1593d16d
made Logs dump with dump 0 or -1
2011-11-27 22:23:02 -08:00
Jason Short
b3bd4bd3c9
Cosmetic cleanup, commented functions for compiler warnings
2011-11-27 22:23:02 -08:00
Jason Short
fb5302c50b
No longer resetting ch7 wp index with mode change, requires reboot
2011-11-27 22:23:02 -08:00
Andrew Tridgell
2cabb11307
mavlink: don't force CLI and HIL with mavlink10 build
2011-11-28 16:22:33 +11:00
Jason Short
940fa9621c
Added minimum Altitude for RTL failsafe
2011-11-26 16:39:29 -08:00
Jason Short
44cb73c9fa
added safety checks for RTL
2011-11-26 16:39:29 -08:00
Jason Short
d0af4e7200
CH7 with params
2011-11-26 16:39:29 -08:00
Jason Short
ec5b080167
Enable RTL
2011-11-26 16:39:29 -08:00
Jason Short
ca5e4bb802
Allow output of system type
2011-11-26 16:39:28 -08:00
Jason Short
1621f3a638
allow CH7 to be set via params
2011-11-26 16:39:28 -08:00
Jason Short
ea911e0bcb
updated failsafe code
2011-11-26 16:39:28 -08:00
Jason Short
19c3c27ed0
Erasing Logs at new FW version detection
2011-11-26 16:39:28 -08:00
Jason Short
52297679c4
sending Mavlink system type
2011-11-26 16:39:28 -08:00
Andrew Tridgell
a048709828
Logs: don't print hundreds of bogus log boundaries
...
this can take quite a long time
2011-11-26 17:02:55 +11:00
Andrew Tridgell
a99bcec762
desktop: report motors armed in desktop build too
...
this helps in autotest
2011-11-25 20:00:19 -08:00
Pat Hickey
6ee477bd8d
ArduCopter: rev version number from 2.0.51 to 2.1.0 Alpha
2011-11-25 20:00:19 -08:00
Andrew Tridgell
38c85c44ae
ArduCopter: rename purple to APM2
2011-11-25 20:00:19 -08:00
Andrew Tridgell
3a542b3ef3
USB-MUX: enable USB MUX switching for ArduCopter
2011-11-25 20:00:19 -08:00
Andrew Tridgell
338445e60c
ArduCopter-HIL: fixed HIL build
...
Logging isn't always enabled
2011-11-25 20:00:18 -08:00
Andrew Tridgell
ffba37d599
desktop: first version of register level SITL support
...
this adds register level emulation of the ADS7844 and the RC
input/output hardware on the APM1, allowing for SITL testing without
enabling HIL in the code
2011-11-25 20:00:18 -08:00
Andrew Tridgell
aa558eb033
fixed a valgrind error
...
this error is harmless, but false positives can disguise real errors
2011-11-25 20:00:18 -08:00
Pat Hickey
eee2da01ac
Arducopter: each motors_ pde uses APM_RC.SetFastOutputChannels
2011-11-25 20:00:18 -08:00
Pat Hickey
ea4c220ee9
APM_RC: OCR register init moved from ArduCopter/radio.pde to lib inits.
2011-11-25 20:00:18 -08:00
Andrew Tridgell
6093db948b
compass: added AP_COMPASS_APM2_SHIELD
...
this makes the orientation clearer
2011-11-25 20:00:18 -08:00
Andrew Tridgell
41caa949ca
fixed InertialSensor stub build
2011-11-25 20:00:18 -08:00
Pat Hickey
1d50bb80fd
hil-sensors ArduCopter: fixes to make hil-sensors build work properly
...
* requires new stub libraries for InertialSensor and PeriodicProcess.
2011-11-25 20:00:18 -08:00
Andrew Tridgell
1e41b4b2b0
timer_scheduler doesn't exist in HIL_MODE_ATTITUDE
2011-11-25 20:00:18 -08:00
Andrew Tridgell
a3701e521a
build: added hlsensors target
2011-11-25 20:00:18 -08:00
Andrew Tridgell
1c20efe4b8
re-organiser sensor declarations
...
this tries to make the #ifdef nesting easier to understand
2011-11-25 20:00:17 -08:00
Andrew Tridgell
2a5a15abce
test: fixed test code for HIL build
2011-11-25 20:00:17 -08:00
Andrew Tridgell
3072fdda85
adc.Init() needs timer_scheduler
2011-11-25 20:00:17 -08:00
Andrew Tridgell
c0898ab3b9
purple: timer_scheduler should be in all builds
2011-11-25 20:00:17 -08:00
Andrew Tridgell
2d8cfc0c3f
test: neaten up the output of the dcm test
2011-11-25 20:00:17 -08:00
Pat Hickey
3131ab16ef
remove BROKEN_SLIDER code
...
use the new CLI_SLIDER_ENABLED option and the "hit ENTER 3 times"
method
2011-11-25 20:00:17 -08:00
Pat Hickey
475afd6ac2
purple: enable dcm test, and fixed imu test to test the IMU API
2011-11-25 20:00:17 -08:00
Pat Hickey
c2972ff1f9
purple: fixed CLI code for non-ADC hardware and no sonar
...
purple hardware does not use the ADC driver
2011-11-25 20:00:17 -08:00
Pat Hickey
63393b206a
purple: added ins test
...
this tests the InertialSensor library API
2011-11-25 20:00:17 -08:00
Pat Hickey
f1bad83d21
purple: fixed system init for purple sensor objects
2011-11-25 20:00:16 -08:00
Pat Hickey
e3027fe54e
purple: pass isr_registry to APM_RC.Init()
2011-11-25 20:00:16 -08:00
Pat Hickey
660174e610
purple: switch ArduCopter to new sensor objects
...
this uses the new sensor abstractions for the purple/APM1 hardware
choice
2011-11-25 20:00:16 -08:00
Pat Hickey
4869ac3385
purple: use the new LED_ON/LED_OFF macros for LED level
...
this gets this right on both APM1 and purple for ArduCopter
2011-11-25 20:00:16 -08:00
Pat Hickey
3f2692d1da
purple: added configuration logic for APM1 versus purple hardware
...
This abstracts the names for LED on/off (due to the different wiring
of LEDs on APM1 and purple), and adds the needed config defines for
the two hardware types
2011-11-25 20:00:16 -08:00
Pat Hickey
90c5eb8487
purple: added defines for APM hardware selection
...
we can now choose APM_HARDWARE_APM1 or APM_HARDWARE_PURPLE
2011-11-25 20:00:16 -08:00
Pat Hickey
cc67062442
build: added new command line build targets
...
this makes it more convenient to build common options
2011-11-25 20:00:16 -08:00
Pat Hickey
5ee5036fa1
purple: added comment for enabling purple hardware
2011-11-25 20:00:16 -08:00
Andrew Tridgell
89d2f0f849
mod barometer.Init() based on hardware
2011-11-25 20:00:15 -08:00
Michael Oborne
0a0b2d32f4
Add rc input to cli planner mode
2011-11-26 11:23:14 +08:00
Jason Short
abe4758c3b
no longer using the raw pressure
2011-11-25 11:34:05 -08:00
Doug Weibel
9ecfac1156
Change ArduCopter DataFlash log file system to new file system which allows overwriting logs.
...
Also changed the feature to dump all DataFlash memory to occur when user requests dumping log "-1"
2011-11-25 07:17:15 -07:00
Jason Short
c5c5884006
v number
2011-11-21 22:13:18 -08:00
Jason Short
89e014c06a
Added alternate alt hold,
...
New ESC Calibration Routine
2011-11-21 22:12:19 -08:00
Jason Short
85a5647f5d
cleanup
2011-11-21 22:11:06 -08:00
Jason Short
6d99e78887
removed unused function
2011-11-20 21:59:55 -08:00
Jason Short
95b797d359
removed the init_esc - reworking the method to avoid the use of the CLI.
2011-11-20 21:24:32 -08:00
Jason Short
5c797e91b5
Better function definition
2011-11-20 20:32:46 -08:00
Jason Short
beeba99b92
Missed a function definition for no_logs option
2011-11-20 20:29:58 -08:00
Jason Short
2600f19172
RTL Yaw hold as default
2011-11-20 12:50:13 -08:00
Jason Short
fbf09dbf2d
Made save WP the default
...
Cosmetic updates
2011-11-20 12:50:12 -08:00
Randy Mackay
f397bae793
ArduCopter Alt Hold - Change to not run get_nav_throttle if manually adjusting altitude with manual_boost - removes possibility of I term running up
...
Tuning - added ability to modify altitude (position, not rate) controller
TradHeli - Fairly large change to how throttle is scaled and collective moves.
2011-11-20 22:30:42 +09:00
Jason Short
17041e5346
my take at a merge to give tridge a head start at Mav1.0
2011-11-20 00:23:40 -08:00
Jason Short
556db68d2d
Made loiter rad smaller in storage
2011-11-20 00:22:53 -08:00
Jason Short
7feecf3220
renamed WP mask
2011-11-20 00:22:53 -08:00
Jason Short
185c2a50ce
added some params from Arduplane to make Mavlink upgrade easier
...
made loiter radius smaller in storage
2011-11-20 00:22:53 -08:00
Jason Short
94ef8a91ff
removed typo
2011-11-20 00:22:52 -08:00
Jason Short
1e855503da
renamed MASK_OPTIONS_RELATIVE_ALT
2011-11-20 00:22:52 -08:00
Jason Short
c6f9c532af
renamed set_command_with_index
2011-11-20 00:22:52 -08:00
Jason Short
b883ff937c
renamed the options_mask
2011-11-20 00:22:52 -08:00
Jason Short
77da1227bb
renamed set_cmd function
2011-11-20 00:22:52 -08:00
Jason Short
10a24f22fa
renamed set_cmd function
2011-11-20 00:22:52 -08:00
Jason Short
aef4db8263
Logging stabilization KP to hunt bug
2011-11-19 16:59:54 -08:00
Jason Short
194778a6f9
Logging APVar saves
2011-11-19 16:59:54 -08:00
Jason Short
90bc03ef99
new DataLog message
2011-11-19 16:59:54 -08:00
Jason Short
56179a24e1
Added Arbitrary data logging
2011-11-19 16:59:54 -08:00
Jason Short
b6adfdb62f
missed ==
2011-11-19 14:42:57 -08:00
Jason Short
eef04a5a54
removed some tests
2011-11-19 14:02:00 -08:00
Jason Short
8e1f311c36
s
...
shortened strings, logging defines updated
2011-11-19 14:01:47 -08:00
Jason Short
8e509b63a7
shortened strings for mem
2011-11-19 14:00:55 -08:00
Jason Short
d02b4342ae
removed some unused code, made output min by default
2011-11-19 14:00:42 -08:00
Jason Short
d1c161ecd0
Upped version
...
added new logging params
added crosstrack gain
re-ordered param inits
2011-11-19 14:00:23 -08:00
Jason Short
39d0df4cef
added param for crosstrack gain defaulted to 4
2011-11-19 13:59:37 -08:00
Jason Short
9bc4328724
Added crosstrack gain and lowered alt hold rate gain
2011-11-19 13:59:15 -08:00
Jason Short
e4f2ad1809
remove PI_crosstrack
2011-11-19 13:58:53 -08:00