Mike Smith
d79f62ce66
Teach the Makefile about the new Arduino sourcefile suffix
2012-01-15 11:51:38 -08:00
Jason Short
e68f9191c9
updated channel notes
2012-01-15 10:24:15 -08:00
Andrew Tridgell
817e7442bd
baro: fixed an integer overflow issue at high altitudes
...
the averaging array was using 16 bit numbers, but we are storing
numbers with 19 significant bits. That caused overflow at high
altitude, and some very interesting altitude graphs!
Thanks to Michael Oborne for spotting this in a log
2012-01-14 19:51:35 +11:00
Randy Mackay
4e9c668315
OpticalFlow - bug fix - highest resolution was incorrectly set as 1200 instead of 1600
2012-01-14 12:34:29 +09:00
Andrew Tridgell
f4490b62c7
DCM: prevent a segmentation fault when compass is not enabled
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when compass is disabled _compass is NULL
2012-01-13 15:48:07 +11:00
Doug Weibel
622217357c
Bug fix for compass.
...
This is a fix for an interesting bug when a DCM matrix reset was added to the ground start. This bug only showed up if (A) a ground start were performed after an air start or due to use of the "Calibrate Gryo" action, (B) if the current orientation were sufficiently different from 0/0/0, and (C.) if the particular magnetometer had sufficiently large offsets. Why did resetting the DCM matrix to 0/0/0 pitch/roll/yaw at ground start cause a bug? The magnetometer offset nulling determines the proper offsets for the magnetometer by comparing the observed change in the magnetic field vector with the expected change due to rotation as calculated from the rotation in the DCM matrix. This comparison is made at 10Hz, and then filtered with a weight based on the amount of rotation to estimate the offsets. Normally it would take considerable time at normal in-flight rotation rates for the offset estimate to converge.
If a DCM matrix reset occurs when the offset nulling algorithm is up and running, the algorithm sees the DCM reset as a instantaneous rotation, however the magnetic field vector did not change at all. Under certain conditions the algorithm would interpret this as indicating that the offset(s) should be very large. Since the "rotation" could also have been large the filter weighting would be large and it was possible for a large erroneous estimate of the offset(s) to be made based on this single (bad) data point.
To fix this bug methods were added to the compass object to start and stop the offset nulling algorithm. Further, when the algorithm is started, it is set up to get fresh samples. The DCM matrix reset method now calls these new methods to stop the offset nulling before resetting the matrix, and resume after the matrix has been reset.
2012-01-12 14:44:24 -07:00
Andrew Tridgell
a6e87915eb
desktop: floating point precision changes from Justin Beech
2012-01-11 21:31:59 +11:00
Jason Short
f43c29e840
fixed type error
2012-01-10 23:43:44 -08:00
Jason Short
ecaf5ac461
sensorSign swicth
2012-01-10 23:43:44 -08:00
Jason Short
d7d04f67e4
AP Rangefinder had some bad characters in it. Converted and cleaned the text files.
2012-01-10 23:42:26 -08:00
Jason Short
9cbfcac802
Made timer unsigned
2012-01-10 23:42:26 -08:00
Pat Hickey
d015e0d6d9
APM_RC & ArduCopter: Change interface to SetFastOutputChannels to use _BV
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* Every use of MSK_CH_n changed to _BV(CH_n)
* Easier to read, and will allow CH_n to be parameterized without needing
a separate macro expansion for the MSK value.
2012-01-09 21:57:01 -08:00
Doug Weibel
22d2db53d8
Repair dataflash test
2012-01-08 21:29:19 -07:00
Jason Short
f6e268395f
allows main code to manually set the integrator value
2012-01-04 09:28:36 -08:00
Andrew Tridgell
54b91ce2f4
sitl: added build targets for different ACM frames
2012-01-04 21:45:46 +11:00
Andrew Tridgell
7aa294eca2
AP_Compass: when I2c fails, don't retry for 1s
2012-01-04 16:35:47 +11:00
Andrew Tridgell
a7a00a35ab
AP_Baro: when I2c fails, don't retry for 1s
2012-01-04 16:35:16 +11:00
Andrew Tridgell
65fbeea6d1
DataFlash: cope with older dataflash chips
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some of the APM2 DataFlash cards use an older chip with only 4096
pages, and a density code of 6. Doug has one of these.
2012-01-04 16:16:35 +11:00
Michael Oborne
6a279138e9
add gps character count.
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this problem happens when the mtk ends up in nmea mode at 10hz. there is no 50ms window of no activity
2011-12-31 13:05:33 +08:00
Michael Oborne
e66e21cf20
remove gps callback in wait loop
2011-12-31 09:35:40 +08:00
Randy Mackay
19ed12444b
GPS - removed GPS_MTK, GPT_NMEA and GPS_UBLOX. All functionality moved to AP_GPS many months ago.
2011-12-30 22:25:00 +09:00
Jason Short
3878ac01ef
removed newlines to clean up code
2011-12-29 23:02:01 -08:00
Randy Mackay
ff66a3417c
OptFlow - initial support for APM2 (there are still problems) including adding ability to set Chip Select pin.
...
Other unrelated changes are:
a) fixed typo in 'esitmate_velocity' to 'estimate_velocity'.
b) moved init_compass from system.pde to sensors.pde which seemed consistent with other sensors.
2011-12-30 12:06:31 +09:00
Andrew Tridgell
671d0b82ad
Baro: fixed MS5611 example sketch
2011-12-28 21:49:29 +11:00
Andrew Tridgell
5f0e070f4e
compass: show timing in compass test
2011-12-28 21:44:18 +11:00
Andrew Tridgell
c448e85ed1
Baro: show timing in baro test
2011-12-28 21:43:52 +11:00
Andrew Tridgell
669a129175
DCM: don't use compass unless its healthy
2011-12-28 20:41:54 +11:00
Andrew Tridgell
603b605eb1
I2C: fixed some warnings
2011-12-28 20:41:53 +11:00
Andrew Tridgell
f4e1f3d54d
desktop: exclude I2C library
2011-12-28 20:41:53 +11:00
Andrew Tridgell
9ef1c421bd
MPU6k: don't init the Wire library
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we don't use Wire any more
2011-12-28 20:41:53 +11:00
Andrew Tridgell
2960abf41f
I2C: convert barometer library to new I2C library
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this also adds a healthy attribute and error checking
2011-12-28 20:41:53 +11:00
Andrew Tridgell
f93c716126
I2C: convert compass code to new I2C library
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this also adds a healthy attribute, and error checking on all I2C
calls
2011-12-28 20:41:53 +11:00
Andrew Tridgell
632e74b76d
I2C: imported the I2C library from Wayne Truchsess
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this gives us a more robust interface, including timeouts
2011-12-28 20:28:31 +11:00
Andrew Tridgell
f8e1d88815
TimerProcess: prevent a race in setting up the timer callbacks
2011-12-28 16:00:49 +11:00
Andrew Tridgell
089470a671
DataFlash: moved high level logging logic to library
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this moves out all the high level logic from ArduPlane/ArduCopter to
the library. It also adds a "config page", as the last page in the
flash. This is used to check if the flash needs erasing. We only erase
now if the DF_LOGGING_FORMAT has changed.
This patch also adds a public CardInserted() method, which is used to
disable logging on APM2 if a dataflash card is not inserted
2011-12-28 16:00:48 +11:00
Andrew Tridgell
42eb62cc46
DataFlash: fixed sense of card detect
2011-12-28 16:00:48 +11:00
Andrew Tridgell
1cb8728a6b
MPU6000: protect the driver from double initialisation
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initialising twice can lockup the driver
2011-12-28 16:00:48 +11:00
Andrew Tridgell
f2bbfb1296
MPU6000: minor fixes
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the hardware functions should be private, and cs_pin should be uint8_t
2011-12-28 16:00:48 +11:00
Andrew Tridgell
d35113f8a6
TimerProcess: check for duplicate registrations
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if a driver gets initialised twice, make sure it doesn't get called
twice in the timer loop
2011-12-28 16:00:48 +11:00
Andrew Tridgell
0a08a0b515
TimerProcess: make some variables uint8_t
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save a couple of bytes
2011-12-28 16:00:48 +11:00
Mike Smith
ac3f7512cc
Fix issue #423 - FastSerial flush bug.
2011-12-26 15:52:21 -08:00
Andrew Tridgell
9f5718bcfa
added in DataFlash.cpp
...
forgot this ....
2011-12-26 19:34:06 +11:00
Andrew Tridgell
887ff43e1f
desktop: added attachInterrupt() support
2011-12-26 19:17:11 +11:00
Andrew Tridgell
22c8db774f
desktop: fixed for new DataFlash inheritance
2011-12-26 19:17:11 +11:00
Andrew Tridgell
dd26ef3089
dataflash: reworked classes to move most code to parent class
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this moves all the non-hardware specific code to the parent
DataFlash_Class class, keeping the hw specific code much smaller and
simpler.
This should prevent discrepancies creeping in between APM1 and APM2
support again
2011-12-26 19:17:11 +11:00
Andrew Tridgell
8bf05982ae
dataflash: fixed APM2 flash logging
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we had log wrap disabled on APM2, and also had the wrong log size. The
mainline code assumed 4096, but it is 8192 pages long.
2011-12-26 19:17:11 +11:00
Andrew Tridgell
df0d151891
MPU6000: change to 98Hz low pass filter
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based on recommendation from Pat
2011-12-26 19:17:11 +11:00
Andrew Tridgell
3ef707a2c3
MPU6000: use data ready interrupt to prevent stale data
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We listen for a data ready interrupt and only read new data in read()
if there is new data
2011-12-26 19:17:11 +11:00
Andrew Tridgell
71e08f8484
fixed the MPU6000 test sketch
2011-12-26 19:17:11 +11:00
Randy Mackay
af121c492d
Merge remote-tracking branch 'origin/master'
2011-12-25 12:34:16 +09:00
Randy Mackay
c3ea1ca5dc
AP_GPS - updated MTK rate to 10Hz and fixed lat/lon printing inaccuracy in Arducopter logs and AP_TEST example sketch
2011-12-25 12:33:06 +09:00
Andrew Tridgell
7c0f39aec5
added MPU6000 test sketch
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this doesn't work yet - Pat, any idea why?
2011-12-25 12:03:39 +11:00
Andrew Tridgell
09c97bb367
removed dead test program
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this one doesn't build, and has been replaced by IMU_MPU6000_test
2011-12-24 18:11:04 +11:00
Andrew Tridgell
f587a01165
ADC: update for new ap_proceduce prototype
2011-12-21 23:31:38 +11:00
Andrew Tridgell
5b75458502
AP_Baro: update MS5611 driver for new ap_proceduce prototype
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this saves calling millis() quite so often
2011-12-21 23:31:38 +11:00
Andrew Tridgell
cef1c4c558
MPU6k: update driver for new ap_proceduce prototype
2011-12-21 23:31:38 +11:00
Andrew Tridgell
8cc2b7669b
PeriodicProcess: added set_failsafe() call
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this adds an optional failsafe function that will be called in the
timer loop
2011-12-21 23:31:38 +11:00
Andrew Tridgell
845683a56c
added comment in polygon code
2011-12-21 23:31:38 +11:00
Andrew Tridgell
eac625ba8f
rollover is not a bug
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subtracting unsigned numbers does the right thing
2011-12-21 23:31:38 +11:00
Andrew Tridgell
eec5f000b5
added code format markers to AP_InertialSensor library
2011-12-21 23:31:38 +11:00
Andrew Tridgell
614aeb274c
fixed build of IMU_MPU6000_test
2011-12-21 23:31:38 +11:00
Andrew Tridgell
b52cd45670
fixed comment
2011-12-19 20:52:59 +11:00
Andrew Tridgell
7c9c26e2b7
AP_Math: re-work polygon algorithm for perfect precision
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using sign checking and 64 bit integer math only when needed results
in an algorithm that is just as fast as the floating point version,
but has perfect results for any representable lat/lng
2011-12-19 18:52:56 +11:00
Randy Mackay
a51e868766
AP_RangeFinder - change sonar example sketch to use default Sonar PIN for APM2 (A1)
2011-12-18 14:15:50 +09:00
Andrew Tridgell
7442ba31d8
polygon: improve the speed and precision of the polygon algorithm
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now takes 156 usec per test, with a 11 point boundary
2011-12-18 12:59:50 +11:00
Michael Oborne
3848f2094e
make file relax
2011-12-17 20:42:51 +08:00
Michael Oborne
fd35ba5976
add relax
2011-12-17 16:53:14 +08:00
Andrew Tridgell
0c8c707980
AP_Baro: fixed temperature on MS5611
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this caused a 2x scaling of altitude
2011-12-17 14:58:58 +11:00
Andrew Tridgell
3654c714e9
Revert "ADC: only read channels that are actually being used"
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This reverts commit 95e6bb26f4772ca8c7faa62215de6f078d3df3c7.
ADC will be disabled on APM2
2011-12-17 07:29:09 +11:00
Andrew Tridgell
c18ad75504
Revert "ADC: added an enable_channel() API"
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This reverts commit dafeac01d8f14162600cf821404ba4072dcae14d.
ADC will be disabled on APM2
2011-12-17 07:29:09 +11:00
Andrew Tridgell
f6a7ad9fa6
Revert "ADC: fixed HIL build"
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This reverts commit 86c1a6a5fdd929516cf0f64f4d610cfcd4b4f774.
ADC will now be disabled on APM2
2011-12-17 07:29:09 +11:00
Andrew Tridgell
7c939e83e0
AnalogSource: return a float from read() method
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this gives the full resolution when using the ADC backend. It also
adds scaling for the Arduino backend
2011-12-17 07:29:09 +11:00
Andrew Tridgell
4bbd5392ef
removed AperiodicProcess code
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this code was never being used, and was more complex than it was
worth.
2011-12-17 07:29:09 +11:00
Andrew Tridgell
04ec569313
ADC: fixed HIL build
2011-12-16 20:58:04 +11:00
Andrew Tridgell
658d1d2ba3
added missing mavlink headers
2011-12-16 20:53:26 +11:00
Andrew Tridgell
1ab2b416a3
geofence: store fence points as int32_t
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this keeps maximum precision in fence boundaries
2011-12-16 20:11:51 +11:00
Andrew Tridgell
2e2b320560
mavlink: include latest geofence message changes
2011-12-16 20:11:51 +11:00
Andrew Tridgell
3ddfc6664a
AP_Math: better polygon algorithm
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this one seems to do better with single precision floating point
2011-12-16 20:11:51 +11:00
Andrew Tridgell
686f96414c
MAVLink: update to latest mavlink XML
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this includes the geo-fencing messages
2011-12-16 20:11:51 +11:00
Andrew Tridgell
c56e5735c2
ADC: added an enable_channel() API
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enable_channel() must be used before the Ch6() method is called to
enable gathering of data on the required channels
2011-12-16 20:09:40 +11:00
Andrew Tridgell
be1ba5354e
timer: enable interrupts during timer processing
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this prevents us losing serial bytes when we call sensor drivers that
take more than 100usec to read.
We also prevent timer recursion by re-enabling the timer after all
callbacks are complete
2011-12-16 20:09:38 +11:00
Andrew Tridgell
af7e34fcc1
ADC: only read channels that are actually being used
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on the APM2 we usually use none of the ADC channels, although we may
use the airspeed sensor. This change means we detect which channels
are being read, and only do the SPI transfers for those ones. That
saves us about 100usec per timer interrupt (ie. about 10% of our CPU)
2011-12-16 20:09:35 +11:00
Andrew Tridgell
9e9b229a1d
fixed formatting of ADC driver
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it was a nasty mix of DOS and UNIX
2011-12-16 20:09:29 +11:00
Andrew Tridgell
5b4717ea55
timers: change to 1kHz timer by default
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we were using a 227Hz timer, which is far too slow
2011-12-16 20:09:25 +11:00
Andrew Tridgell
6ad5df2958
desktop: fixed type of dword eeprom read
2011-12-16 20:09:18 +11:00
Andrew Tridgell
338fb1642a
AP_Math: make out vector and matrix elements used types with fixed sizes
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this prevents differences between CPU types
2011-12-16 20:09:11 +11:00
Pat Hickey
291aaffdd9
APM_RC_APM2: Remove OutputCh from ::Init()
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* These calls were off by one anyway, by using the channel numbers
as ints ant not CH_n macros, and that caused an ESC cal problem.
2011-12-15 13:47:43 -08:00
Andrew Tridgell
f4bd3cb5a2
AP_Math: added Polygon_complete() function
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used to veryify user supplied boundaries
2011-12-15 14:42:34 +11:00
Andrew Tridgell
cd9fb3c47a
AP_Math: added a Polygon_outside() function
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this tests if a point is outside of a polygon. This will be used as
part of our geo-fencing support, and also for a new 'fenced mode'
2011-12-15 14:34:58 +11:00
Andrew Tridgell
621f21e4f5
DCM: added matrix_reset() method
2011-12-13 21:32:50 +11:00
Andrew Tridgell
919ae17473
IMU: abstract the setting of the LEDs in IMU initialisation
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we need this to cope with different LED pin assignments on APM1/APM2
2011-12-13 18:19:12 +11:00
Andrew Tridgell
9548366a91
autotest: make magnetic field point down
2011-12-12 22:14:01 +11:00
Andrew Tridgell
fa83de98c8
desktop: fixed build with new AP_Baro code
2011-12-12 15:14:55 +11:00
Andrew Tridgell
eaf134e47e
desktop: fixed desktop barometer code
2011-12-12 15:14:55 +11:00
Andrew Tridgell
de5c1c5147
barometer: fixed HIL barometer build
2011-12-12 15:14:55 +11:00
Andrew Tridgell
47da2ec992
ADC: change adc.Ch() to return a float
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this gives us a bit more precision in airspeed measurement, and costs
us virtually nothing as we are converting to float immediately after
getting the value
2011-12-12 15:14:55 +11:00
Andrew Tridgell
43a53aa303
dcm: fixed an uninitialised variable
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if no compass and not in motion the DCM we would multiply by an
uninitialised number
2011-12-11 15:21:10 -08:00
Pat Hickey
5819f99986
AP_Baro_MS5611: Asynchronous operation, plus c++ style changes.
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Yeah, I know this was a big change to make all at once.
2011-12-11 15:21:10 -08:00
Pat Hickey
3d882c4d49
AP_Baro : Add init( AP_PeriodicProcess * ) method to interface & implementations
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AP_Baro_MS5611 and AP_Baro_BMP085 implement the interface, with stubs only
2011-12-11 15:21:10 -08:00
Pat Hickey
d5386b8bb8
AP_Baro_BMP085: move apm2_hardware flag from init to constructor.
2011-12-11 15:21:10 -08:00