Jason Short
0a7378856d
Added finish to missions - auto-land or stabilize
2012-01-07 22:27:26 -08:00
Jason Short
cf5e0b3a1b
converted auto land to use the mission planner version
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Removed gate that looked for already set control_mode. Wasn't compatible with failsafe
2012-01-07 22:27:26 -08:00
Jason Short
12493d6431
Moved wind comp into a define
2012-01-07 22:27:26 -08:00
Jason Short
7e96e0f7fa
Quad frame - X is default
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added wind comp stability option to config - off by default
2012-01-07 22:27:26 -08:00
Jason Short
250545f31d
Auto-land updates - removed sonar option - not needed
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updates from JLN
2012-01-07 22:27:26 -08:00
Jason Short
ca80dc549c
Made RTL hold position until it reaches altitude
2012-01-07 22:27:26 -08:00
Jason Short
b8bcd81b39
Cleanup
2012-01-07 22:27:26 -08:00
Jason Short
048532ae98
scaled to 0-1023
2012-01-06 21:43:37 -08:00
Chris Anderson
5aab7d583c
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2012-01-06 12:32:39 -08:00
Jason Short
058a3275c3
Revved to R7
2012-01-06 10:22:53 -08:00
Jason Short
056a08d838
Forced Faildafe throttle mode to throttle Auto
2012-01-06 10:21:50 -08:00
Jason Short
57c3405658
Added check for armed motors in failsafe
2012-01-06 10:21:23 -08:00
Jason Short
a640311f58
Added Note
2012-01-06 10:20:59 -08:00
Jason Short
e908390c64
Made RTL go up 10m for failsafe
2012-01-06 10:20:48 -08:00
Jason Short
d430c847fa
Changed default throttle type for failsafe to avoid checking
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changed timer to 20 seconds.
2012-01-06 10:20:31 -08:00
Jason Short
de912b5054
Auto_land update
2012-01-05 21:57:34 -08:00
Jason Short
beac2930c9
Added auto_land to RTL
2012-01-05 21:15:12 -08:00
Jason Short
9d9bef37a8
Clears Auto_land timer
2012-01-05 21:15:12 -08:00
Chris Anderson
d94562986f
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2012-01-05 09:48:32 -08:00
Jason Short
a8af509517
timer set to unsigned
2012-01-04 17:31:20 -08:00
Andrew Tridgell
600a5680f8
ACM: reset all I terms on gyro calibration
2012-01-05 10:15:14 +11:00
Andrew Tridgell
a6808162d6
ACM: fixed a warning
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comment out some unused debug code
2012-01-05 10:14:53 +11:00
Andrew Tridgell
734b0a02be
ACM: fixed a alt hold bug
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== instead of =
2012-01-05 10:14:30 +11:00
Andrew Tridgell
3c965ff1a2
ACM: fixed a signed/unsigned warning
2012-01-05 10:14:12 +11:00
Andrew Tridgell
9ee3431928
ACM-simple: don't use uninitialised simple trig values
2012-01-05 10:13:36 +11:00
Jason Short
8341a080ce
Disabled stable mode wind comp by default for release
2012-01-04 09:28:38 -08:00
Jason Short
5aa0861ec2
Added Xplane output option
2012-01-04 09:28:38 -08:00
Jason Short
6b9d35cc34
Added home offset for altitude
2012-01-04 09:28:38 -08:00
Jason Short
f74e265bb9
Made landing disarm the motors
2012-01-04 09:28:38 -08:00
Jason Short
3ac37c09a9
Upped Revision
2012-01-04 09:28:38 -08:00
Jason Short
a70fdc58a1
Cleaned up and documented each global vavriable
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Added Wind compensation for Stability
Acro mode fixes
2012-01-04 09:28:37 -08:00
Jason Short
123ce533bb
Added precalc for wind compensation when entering Stabilze mode
2012-01-04 09:28:37 -08:00
Jason Short
bf8e3975ec
Added Wind compensation for Stabilize
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moved speed calc to it's own function
decreased acceleration from WPs
2012-01-04 09:28:37 -08:00
Jason Short
6b3094e053
removed PM test field 1 - not needed
2012-01-04 09:28:37 -08:00
Jason Short
7858976407
removed unused vars
2012-01-04 09:28:37 -08:00
Jason Short
22c3853020
removed unused vars
2012-01-04 09:28:37 -08:00
Jason Short
e5994c578a
removed unused vars
2012-01-04 09:28:37 -08:00
Jason Short
3d7f3f6b77
removed unused var
2012-01-04 09:28:37 -08:00
Jason Short
8d63af2a89
removed airspeed
2012-01-04 09:28:37 -08:00
Jason Short
a1c3ce88a0
calc_wind_compensation called when exiting AP modes
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Rate I terms reset in Acro Mode switch
Limit of 1 m set to alt hold
Reset circle angle to 0 by default
Land got land_complete var set to false by default
2012-01-04 09:28:37 -08:00
Jason Short
e6887aa3ec
added Reset_Rate_I function
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Removed I term from Throttle rate calc
Added some basic constrains to Acro
2012-01-04 09:28:37 -08:00
Jason Short
dd4b4c723a
removed airspeed
2012-01-04 09:28:37 -08:00
Jason Short
7bef298a46
cleanup - removed unused functions, made pressure reading Float to avoid extra cast
2012-01-04 09:28:36 -08:00
Jason Short
d7f4328441
cosmetic
2012-01-04 09:28:36 -08:00
Jason Short
1883d0c1a8
Added takeoff state and ground state variable
2012-01-04 09:28:36 -08:00
Jason Short
c629795050
Cosmetic
2012-01-04 09:28:36 -08:00
Jason Short
801b3a8e8f
removed unused Airspeed config
2012-01-04 09:28:36 -08:00
Jason Short
fcd18d5538
Removed unused options
2012-01-04 09:28:36 -08:00
Jason Short
525ac4df88
Cosmetic
2012-01-04 09:28:36 -08:00
Jason Short
c450cc4e92
removed unused Airspeed config
2012-01-04 09:28:36 -08:00
Jason Short
4a50e08ac1
change how Reset Nav params work - no longer clear I terms
2012-01-04 09:28:36 -08:00
Jason Short
fe265b3040
Added JLN's landing patch, moved some variables local such as Jump counter
2012-01-04 09:28:36 -08:00
Jason Short
5de709ceea
removed unused functions
2012-01-04 09:28:36 -08:00
Andrew Tridgell
54b91ce2f4
sitl: added build targets for different ACM frames
2012-01-04 21:45:46 +11:00
Andrew Tridgell
d6ccffc71b
ACM: don't set defaults in APM_Config.h
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defaults set here prevent Makefile overrides, which breaks autotest
for non-default frame types
2012-01-04 19:35:05 +11:00
Chris Anderson
33f4cde5c3
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2012-01-03 22:11:22 -08:00
Andrew Tridgell
645eac6f38
I2c: default to 5ms timeout, and faster bus speed
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we will slow down the speed when we get a failure
2012-01-04 16:36:47 +11:00
Chris Anderson
1cfb7ecf7c
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2011-12-31 20:09:26 -08:00
Jason Short
24bddb1c47
Added more constraints around velocity
2011-12-31 10:59:59 -08:00
Jason Short
86e01fce17
Cosmetic
2011-12-31 10:54:31 -08:00
Jason Short
bfd7608f4d
Lowered Yaw to prevent overshoot based on feedback
2011-12-31 10:10:45 -08:00
Jason Short
e8db2225dd
upped to r5
2011-12-31 10:05:13 -08:00
Chris Anderson
31765310ac
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2011-12-31 09:50:33 -08:00
Jason Short
e17c8705ba
Loiter I reset
2011-12-31 09:45:25 -08:00
Jason Short
e9d41897df
R4
2011-12-30 23:54:02 -08:00
Jason Short
1d636219f9
New Style WP navigation for high wind
2011-12-30 23:48:05 -08:00
Jason Short
fc93a73ad7
no longer calling reset_nav
2011-12-30 23:48:04 -08:00
Jason Short
170a646ecf
removing I term clearance
2011-12-30 23:48:04 -08:00
Jason Short
4b2979743f
no longer calling reset_nav
2011-12-30 23:48:04 -08:00
Jason Short
62ca68cdbb
Reverted to Crosstrack like in Arduplane, requires Degrees * 100
2011-12-30 23:48:04 -08:00
Jason Short
27d3564eab
Sync with Arduplane
2011-12-30 23:48:04 -08:00
Jason Short
f5ffa7bd7e
Updated Configs based on field testing.
2011-12-30 23:48:04 -08:00
Jason Short
e08b550f44
Added a default Yaw tracking setting
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Added Nav_Bearing
2011-12-30 23:48:04 -08:00
Jason Short
09db32ee02
Added Nav_bearing, just like APlane
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added fix for LOITER in missions so we don't Yaw in circles
2011-12-30 23:48:04 -08:00
Jason Short
758a5240f2
removed old loiter method option
2011-12-30 23:48:04 -08:00
Chris Anderson
47eedcdfa1
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2011-12-30 22:53:23 -08:00
Randy Mackay
c39ebde9de
ArduCopter - init_compass - fixed HIL build issue
2011-12-31 12:29:54 +09:00
Chris Anderson
4e1b140c57
Merge branch 'master' of https://code.google.com/p/ardupilot-mega
2011-12-30 09:31:05 -08:00
Jason Short
57b2d17d8a
updated rev
2011-12-29 23:02:41 -08:00
Jason Short
8fc73844ee
Yaw Performance tweaks
2011-12-29 23:02:03 -08:00
Jason Short
4535bc4fd9
lowered to nav_lat and nav_lon int16
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added a version that didn't have I term added to get a better indication of velocity estimation
2011-12-29 23:02:03 -08:00
Jason Short
89c705c8b9
removed loiter I from Reset Nav
2011-12-29 23:02:03 -08:00
Jason Short
723adffc48
updated Loiter gains
2011-12-29 23:02:03 -08:00
Jason Short
4bfa5def76
removed Rate_I from Loiter, lowing Rate_P from Loiter too. Too aggressive leads to rapid oscillations in air, and not around loiter position.
2011-12-29 23:02:03 -08:00
Jason Short
2f657ebdbf
cosmetic
2011-12-29 23:02:03 -08:00
Jason Short
aa2e474b80
Added 5 sec Takeoff Timer to clear i terms when lifting
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Moved loiter relocation function to update_nav
moved User hooks to correct place
Added tuning for D term
2011-12-29 23:02:03 -08:00
Jason Short
8a1b9df325
Added Stabilize_D parameter
2011-12-29 23:02:02 -08:00
Jason Short
ce990f3050
Upped Yaw speed to deal with performance complaints
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Added new Stabilize D term default of .25
2011-12-29 23:02:02 -08:00
Jason Short
83d52899b0
Added second order, filtered derivative in stabilize. Works much better than the non-filtered one I used to have.
2011-12-29 23:02:02 -08:00
Jason Short
e42d5cb4f9
Fixes for Smooth Loiter
2011-12-29 23:02:02 -08:00
Jason Short
c4ad864ed0
Set Define for Max throttle
2011-12-29 23:02:02 -08:00
Jason Short
737feabc6c
Fixed a 1280 only test
2011-12-29 23:02:02 -08:00
Jason Short
f94727ed02
added define for Max throttle
2011-12-29 23:02:02 -08:00
Jason Short
200f7da103
Added Dampening term for tuning
2011-12-29 23:02:02 -08:00
Jason Short
80e1715b12
updated Loiter PIDs
2011-12-29 23:02:02 -08:00
Jason Short
db0a7be233
Enable Magnetometer by default
2011-12-29 23:02:02 -08:00
Jason Short
3202f1cf64
Missing ;
2011-12-29 23:02:01 -08:00
Jason Short
9832d8eccb
removed takeoff complete flag from missions, not used and would be useful elsewhere.
2011-12-29 23:02:01 -08:00
Jason Short
9f7aae5945
removed unused function
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Simplified the baro init filter
2011-12-29 23:02:01 -08:00
Randy Mackay
ff66a3417c
OptFlow - initial support for APM2 (there are still problems) including adding ability to set Chip Select pin.
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Other unrelated changes are:
a) fixed typo in 'esitmate_velocity' to 'estimate_velocity'.
b) moved init_compass from system.pde to sensors.pde which seemed consistent with other sensors.
2011-12-30 12:06:31 +09:00