Commit Graph

1019 Commits

Author SHA1 Message Date
rmackay9
599cea21bb Added multiple new tuning parameters to the inflight channel 6 tuning feature:
#define CH6_YAW_KI 24
        #define CH6_ACRO_KP 25
        #define CH6_YAW_RATE_KD 26
        #define CH6_LOITER_KI 27
        #define CH6_LOITER_RATE_KI 28
2012-03-28 23:58:58 +09:00
Andrew Tridgell
34506b170f Mavlink: fixed warnings about limits on int32 values 2012-03-27 15:37:25 +11:00
Andrew Tridgell
e0c9ab5a29 ACM: fixed heli build 2012-03-27 15:37:25 +11:00
Andrew Tridgell
47f9dfd125 ACM: fixed the build on the 1280 2012-03-27 15:37:24 +11:00
Andrew Tridgell
e956e21e7d ACM: enable the new compass offset nulling in ACM 2012-03-27 15:37:24 +11:00
rmackay9
1f4cfb9333 ArduCopter - added PID log type. Implemented for Yaw stabilize and rate controllers. 2012-03-25 16:09:08 +09:00
rmackay9
67cf7b9eed ArduCopter - updated firmware version to 2.5.3 2012-03-25 09:13:51 +09:00
rmackay9
63b96c0153 ArduCopter - altitude hold - ensure throttle_avg is initialised from g.throttle_cruise parameter 2012-03-23 23:48:24 +09:00
rmackay9
89576a281a ArduCopter - updated to firmware version to 2.5.2 to avoid confusion with post 2.5.1 versions posted to downloads area 2012-03-23 23:12:49 +09:00
Robert Lefebvre
84d8414a2e Fix Auto_Trim to allow it to actually be called when setup on Ch7 pulldown menu in MP. 2012-03-23 09:17:58 -04:00
Jason Short
e2560c5865 Throttle_hold was in APM_Config - which is ignored by the Mission planner Hex generator 2012-03-22 10:01:24 -07:00
rmackay9
ad4a2aa9f3 ArduCopter - motors_quad.pde - corrected test sequence for + configuration 2012-03-21 22:04:50 +09:00
rmackay9
66c4f752e3 ArduCopter - navigation - corrected comment in check_missed_wp function to clarify that you've passed the waypoint when the direction to the way point is more than 100 degrees off (not 10 degrees off) from your original bearing towards the waypoint 2012-03-20 17:11:22 +09:00
rmackay9
1dd554c333 ArduCopter - updated version to 2.5.1 2012-03-20 17:08:18 +09:00
rmackay9
0773a25b5d ArduCopter - increased default THROTTLE_CRUISE to 450 2012-03-20 16:34:07 +09:00
rmackay9
22315cd41a ArduCopter - Navigation.pde - corrected comment re wp_distance and get_distance to clarify that they are in cm (not meters!) 2012-03-20 16:13:38 +09:00
Andrew Tridgell
458d55e5bc MAVLink: constrain variable changes to the datatype range
if someone tries to set a AP_Int16 to a value of 300000, they now get
32767 instead of -27678
2012-03-19 17:29:02 +11:00
Andrew Tridgell
547b4ed55b AHRS: adapt ArduCopter for new AHRS framework 2012-03-19 17:29:02 +11:00
Jason Short
c5344a2a85 ACM: Arducopter.pde - Added a constraint to the NO_NAV mode to be similar to the Loiter and rate nav modes. 2012-03-18 22:31:22 -07:00
Jason Short
a0717f082e ACM: Attitude.pde - consolidated wind I term resets 2012-03-18 22:31:21 -07:00
Jason Short
fe7ca98701 ACM: system.pde - removed reset_nav_I() to consolidate the wind control reset. 2012-03-18 22:31:21 -07:00
rmackay9
9841cb0335 ArduCopter - small change to ensure both roll and pitch commands are zero before switching out of loiter_override (loiter override becomes true when roll+pitch command is greater than 5 degrees and switches back to false when both become zero)
- remove incorrect comments about when loiter target position is reset.
2012-03-18 15:16:04 +09:00
rmackay9
dc92da818c ArduCopter - remove reference to AUTO_RESET_LOITER that is not used anymore 2012-03-18 14:53:19 +09:00
rmackay9
91b2b48fd8 ArduCopter - bug fix to calc_XY_velocity (was using uninitialised last_longitutde and last_latitude for speed calculations) 2012-03-18 12:11:12 +09:00
Jason Short
491af02d8a ACM: Lowered gains from flight tests today with 3DR Quad 2012-03-17 11:04:01 -07:00
Jason Short
427dacba70 ACM: Smoother Speed calcs 2012-03-16 14:10:19 -07:00
Jason Short
3038da1dc3 ACM: Softer Loiter Gains 2012-03-16 14:10:19 -07:00
Jason Short
48a0c9a818 ACM: Small fix to nav_throttle to prevent too fast of a landing. 2012-03-16 14:10:19 -07:00
Jason Short
6201bdb8a7 ACM: Fixed comment 2012-03-16 14:10:19 -07:00
Jason Short
1c0b28c956 Fixed Scaling bug in Sonar mixing 2012-03-16 14:10:19 -07:00
Jason Short
7153b94ade ACM: Disabled D term experiment for Loiter until more testing 2012-03-15 19:20:03 -07:00
Jason Short
a52a14bf12 Tune down Loiter_P a hair 2012-03-15 19:17:27 -07:00
Robert Lefebvre
be3fe36c52 Small fix on the Traditional Helicopter Collective-Yaw compensation calculation. 2012-03-15 20:14:18 -04:00
rmackay9
68e37774a6 ArduCopter - removed #define AUTOMATIC_DECLINATION ENABLED line to ensure users don't try and enable it because it needs a bit more work before it's ready for general use 2012-03-15 21:58:42 +09:00
analoguedevices
86eff20d5d Rev'ed version number to 2.5. Added more credits 2012-03-15 02:38:54 +00:00
Jason Short
6f8b97bf6a ACM: Added constraints for invalid climb rates. Robert Lefebvre had a bad sonar and very invalid rates crept into the system. 2012-03-13 21:31:16 -07:00
Jason Short
4315c06f34 Lowering the D filter for less latency and less oscillation. 2012-03-13 12:58:46 -07:00
Jason Short
48ba24a810 ACM: Loiter tuning updates, turned up I a bit, a higher I will work better if the system is well tuned. 2012-03-13 10:23:31 -07:00
Jason Short
468d9c4b4f ACM: Loiter D performance updates 2012-03-13 10:23:31 -07:00
Jason Short
7953808d14 ACM: Larger filter for Loiter D 2012-03-13 10:23:30 -07:00
Jason Short
7034b709d1 ACM: removing old define 2012-03-12 13:11:30 -07:00
Jason Short
73e2bd6cd8 ACM: Got the sign wrong. I'm using the derivative of the error now and not the sensor, so the sign was reversed. 2012-03-12 13:11:05 -07:00
Jason Short
0b51d9b8b0 ACM: Made Loiter_D 0 by default. Accidentally left it on by default. 2012-03-12 10:37:15 -07:00
Jason Short
deed802d1a ACM: Broke out the D term for the PID loop to add custom filtering. The current AC_PID filtering wasn't working for this application and we needed more smoothing. Bad pitch oscillations were being transmitted to the copter. 2012-03-11 23:21:49 -07:00
Jason Short
b3795f1c00 ACM: removed Filtering code for motors in Quad for testing 2012-03-11 23:21:49 -07:00
Jason Short
a989b88680 ACM: made same as Loiter I 2012-03-11 23:21:49 -07:00
Jason Short
0d434ca92c ACM: Tuning based on flights today 2012-03-11 23:21:49 -07:00
Jason Short
0ab6b6e592 ACM: Rate_d filter for PID loop of Loiter. 2012-03-11 23:21:49 -07:00
Jason Short
77fe7de55d ACM: The I term in update_nav_wp with the no_nav condition was pulling from the wrong PID loop and was essentially 0 all the time. 2012-03-11 23:21:49 -07:00
rmackay9
a869a01294 ArduCopter - Log.pde - added wrap_360 to compass heading field of ATT message to resolve overflow problem that caused heading to appear as being off by 70 degrees 2012-03-12 12:09:04 +09:00