forked from Archive/PX4-Autopilot
53bc357cda
This updating of the driver setting is for EMI issue with GPS and FCC. With this setting the clock is sinusoidal N.B. sd_bench fails on SanDISK HC, but Passes SanDISK **HC1** and Kingston cards. ****Use HC1 or Kingston cards!*** Testing done on SanDISK HC all failed sd_bench with Drive/Slew other than default and _PIN_OUTPUT_FAST|_PIN_OUTPUT_HIGHDRIVE _PIN_OUTPUT_FAST|_PIN_OUTPUT_HIGHDRIVE Square noisy, pass SanDISK HC _PIN_OUTPUT_FAST|_PIN_OUTPUT_LOWDRIVE Square noisy, pass SanDISK HC _PIN_OUTPUT_HIGHDRIVE|_PIN_OUTPUT_SLOW sinusoidal fail SanDISK HC, pass SanDISK HC1 _PIN_OUTPUT_LOWDRIVE |_PIN_OUTPUT_SLOW sinusoidal fail SanDISK HC, pass SanDISK HC1 _PIN_OUTPUT_SLOW sinusoidal fail SanDISK HC, pass SanDISK HC1 |
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aerotenna/ocpoc | ||
airmind/mindpx-v2 | ||
atlflight | ||
atmel/same70xplained | ||
auav | ||
av/x-v1 | ||
beaglebone/blue | ||
bitcraze/crazyflie | ||
emlid/navio2 | ||
gumstix/aerocore2 | ||
intel/aerofc-v1 | ||
nxp/fmuk66-v3 | ||
omnibus/f4sd | ||
parrot/bebop | ||
px4 | ||
stm | ||
thiemar/s2740vc-v1 |