Ricardo de Almeida Gonzaga
5e45c9dfb0
waf: add cxx_checks tool
...
In order to start generating AP_Config header and detect
parameter such as the existence of cmath functions.
2016-04-05 20:44:15 -07:00
Ricardo de Almeida Gonzaga
14dbc16d46
waf: start using 'AP_Common/missing' to all boards
2016-04-05 20:44:15 -07:00
Francisco Ferreira
637c3902b4
travis: remove Travis cache since it isn't used currently
2016-04-05 20:27:53 -07:00
Andrew Tridgell
97a7192f76
Plane: make it more obvious that AUTO_FBW_STEER is not for normal use
2016-04-06 07:58:23 +10:00
Grant Morphett
2c4aaf7cb3
Rover: Commit for Rover release 3.0.0
2016-04-05 15:45:18 +10:00
Grant Morphett
801ced34a5
Rover: added the VIBRATION message which is sent to the GCS.
2016-04-05 15:41:53 +10:00
Grant Morphett
8e69b66cf0
Rover: added the VIBE logging to the Dataflash logs.
2016-04-05 15:41:53 +10:00
Saloni Jain
ff74792fd4
Rover: MAV_CMD_DO_SET_HOME support in APMRover2
2016-04-05 15:40:33 +10:00
Andrew Tridgell
981f5a132e
README: added Peter as Tools maintainer
2016-04-05 12:09:09 +10:00
Andrew Tridgell
6c8f0ffad4
mavlink: update submodule
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merged latest from upstream
2016-04-05 11:43:24 +10:00
Peter Barker
009bb7fa9c
build_binaries: regenerate manifest after building binaries
2016-04-05 09:05:57 +10:00
Peter Barker
d7977dfcc2
Tools/scripts/generate-manifest.py: json description of binaries directory
2016-04-05 09:05:57 +10:00
Andrew Tridgell
a8ca41abf1
autotest: use 60% engine speed for stability test
...
can't handle 55% in SITL now in quad
2016-04-04 11:28:28 +10:00
Andrew Tridgell
9db618c73c
AP_AHRS: disable EKF1 for plane
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we are running too close to the 1MByte limit for pixhawk. This
recovers nearly 100kbyte of flash
2016-04-04 11:08:03 +10:00
Andrew Tridgell
5f1ad68bd9
Plane: improved velocity controller for quadplane landing
2016-04-04 09:50:35 +10:00
Andrew Tridgell
8b30569ad1
Plane: setup quadplane earlier in startup
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this ensures the GCS gets the full parameter list as the param count
will be set before mavlink starts
2016-04-03 06:49:38 +10:00
Andrew Tridgell
5cc4b20c73
Plane: smooth out final descent for landing
2016-04-02 22:45:51 +11:00
Andrew Tridgell
7dcd17a2fa
SITL: make multicopter motors only effective above 10%
2016-04-02 22:45:05 +11:00
Andrew Tridgell
6bff07397e
AP_Math: added linear_interpolate() function
2016-04-02 22:44:47 +11:00
Andrew Tridgell
197cefaaa7
Plane: prevent large nose-down on start of velocity controller
2016-04-02 21:19:06 +11:00
Andrew Tridgell
ae51e51c6a
Plane: use velocity controller for initial quadplane landing
2016-04-02 20:54:01 +11:00
Andrew Tridgell
b1266603a6
Plane: setup immediate pitch limit on quadplane takeoff
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this prevents a single loop with large pitch down demand
2016-04-02 19:53:48 +11:00
Andrew Tridgell
602ff03c41
AP_TECS: limit both negative and positive pitch on quadplane transition
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this makes for smoother auto takeoff
2016-04-02 19:53:16 +11:00
Andrew Tridgell
ae5b8849ec
autotest: added CMAC VTOL mission
2016-04-02 16:44:50 +11:00
Andrew Tridgell
27934a893e
autotest: raise timeout again
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after trying lots of other things to speed up build_binaries.sh it
still isn't fast enough, so this just raises the timeout by 50%
2016-04-02 07:47:16 +11:00
Andrew Tridgell
913cf9dd37
Plane: set min quad throttle to 10%
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fixes spin when armed
2016-04-01 22:18:51 +11:00
Andrew Tridgell
7f85c14c96
Plane: fixed landing detector for new AP_Motors code
2016-04-01 21:54:32 +11:00
Andrew Tridgell
70679a06aa
Plane: fixed quadplane throttle control in AUTO
2016-04-01 17:29:51 +11:00
Andrew Tridgell
52cc369f15
Plane: fixed typo in AP_Motors conversion
2016-04-01 16:45:01 +11:00
Andrew Tridgell
e7f7afcc4d
Plane: added correct filter defaults
2016-04-01 16:44:49 +11:00
Andrew Tridgell
9cf909607f
Plane: setup reasonable quadplane defaults
2016-04-01 16:40:06 +11:00
Andrew Tridgell
86416e8f05
AP_Param: added set_default_by_name()
2016-04-01 16:39:51 +11:00
Andrew Tridgell
dd6c4d6225
Plane: fixed up parameters for quadplane
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this fixes quadplane parameters for the new AP_Motors code
2016-04-01 16:17:07 +11:00
Andrew Tridgell
0530af93aa
AP_Param: allow top level parameters to be pointers
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this will allow for the attitude_control variable in quadplane to be a
pointer
2016-04-01 16:16:03 +11:00
Randy Mackay
b96ea15220
Plane: quadplane uses AC_AttitudeControl_Multi
2016-04-01 11:59:30 +09:00
Randy Mackay
87399776a3
AC_PosControl: hover throttle default to 0.5
2016-04-01 11:59:30 +09:00
Randy Mackay
41b584ac9e
Plane: fix quadplane qstabilize throttle input
2016-04-01 11:59:30 +09:00
Randy Mackay
52caed2573
Plane: QTUN df messages angle boost field as float
2016-04-01 11:59:30 +09:00
Randy Mackay
f6eabfdab2
AP_MotorsMulticopter: formatting fixes
2016-04-01 11:59:30 +09:00
Randy Mackay
6807b961e2
AP_MotorsMulticopter: protect against div-by-zero if MOT_SPIN_ARMED is zero
2016-04-01 11:59:30 +09:00
Randy Mackay
b39798ad90
AP_Motors: remove unused DESIRED_SPIN_MIN_THROTTLE
2016-04-01 11:59:30 +09:00
Randy Mackay
dc86e1472c
AP_MotorsTri: protect against div-by-zero if MOT_YAW_SV_ANGLE param was set to 90
2016-04-01 11:59:30 +09:00
Randy Mackay
9b5b6f3779
AP_MotorsHeli: constrain filtered throttle
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This is required because we have removed the constraint on the throttle input. This also insures that there is no lag caused by the filtered throttle straying far outside the 0 to 1 range
2016-04-01 11:59:30 +09:00
Randy Mackay
b4a61e6ccf
AP_Motors: remove constrain on throttle input
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This constraint is redundant because we already constrain the filtered throttle
2016-04-01 11:59:30 +09:00
Leonard Hall
fce426409e
AP_MotorsTri: fix stab patch
2016-04-01 11:59:30 +09:00
Randy Mackay
49562c5ca3
AP_MotorsMulticopter: reduce num bits used for spool-up-down-mode
2016-04-01 11:59:30 +09:00
Andrew Tridgell
c035ade402
Copter: removed slow_start() from throw mode
2016-04-01 11:59:30 +09:00
Randy Mackay
3ee88fd8c7
AP_MotorsCoax: remove output_min
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This is now implemented by parent AP_MotorsMulticopter
2016-04-01 11:59:30 +09:00
Randy Mackay
8566a61660
AP_MotorsSingle: remove output_min
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This is now implemented by parent AP_MotorsMulticopter
2016-04-01 11:59:30 +09:00
Randy Mackay
8621774040
AP_MotorsTri: remove output_min
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This is now implemented by parent AP_MotorsMulticopter
2016-04-01 11:59:30 +09:00